Sentinel
|
Restoration of Sentinel STC6-44 bus
|
|
| Buses & Waggons from Sentinel |
Huddersfield Passenger Transport Group
|
|
|
|
|
|
RESTORATION OF EX EDWARDS CRYMMYCH SENTINEL STC6-44 BUS ODE182 The ODE182 Sentinel Preservation Story So Far by John S. Hinchliffe A Sentinel 44 seat bus was advertised by Peter Bowers in the H.C.V.S. magazine in the summer of 1997, I rang him and discussed the vehicle, from what he said it was to going to be expensive proposition to buy, restore and to bring it to our premises.
Although I was interested mainly because I used to travel on one
to the swimming bathes from our school in the early sixties, this one was owned
by Baddeley Bros of Holmfirth,
At this time it was decided if anyone else was interested to sell it to them but I did say that I would contact him later in the year to find out if it had been sold. When I contacted him November it had not been sold so I said that I would come and have a look at the bus, a few weeks later I went down to a quarry near Aldershot where the bus was along with Lenny Spence and John Shearman.
What we found was slightly worse than I had expected, but a through examination was done taking photographic details to help with anticipated restoration, it was found that the body frame and integral chassis were quite sound, but the floor was rotten and was like walking on a sponge. The gearbox side cover and selectors was missing, the exhaust system was missing, the trackrod was missing, most seats were missing (but Peter had acquired some modern bus seats for the bus but these were green and considered unsuitable as the original seats were red, the green seats are now available for sale from myself).
The engine appeared to be all there apart from one top cover clamp, the injectors and injector pipes, Peter had had the injectors overhauled and these were with some spares including a overhauled pump Peter provided with the bus, the oil was checked and appeared alright although slightly over full one oil pipe was rusted through no further checks could be made on the engine at this time.
Steel corrosion at the front of the bus and cab area was bad, some windows were broken, most panels around the bus were damaged, but the roof was in good shape except for one joint that had been leaking water and causing the wood in the rack bases to rot.
One strange but good point was that where steel had been bolted or riveted together there was no corrosion, this meant that exceptionally high quality aluminium was used by Welsh Metal Industries who it is believed were involved with building the Sentinel integral body, Sentinel's parent company, a design that had been based on a Beadle design that had been used for earlier Sentinel buses. Later that day we looked at various photos of Sentinels and other Sentinel products that Peter had, John, Lenny and myself then went for refreshment, where we looked at photos John had of Sentinel buses, as John lived in the south he would soon be home but Lenny and myself then had the long drive home to Yorkshire.
It was then decision time which depended on the cost of the bus and the cost of getting it home and thanks to Geoff Ripley the Barnsley bus dealer suitable deals were done, which includes the sale of the remains Blackpool 510, which was giving up its place in our arch for the Sentinel so the bus was collected in January 1998. We set off from Boulderbridge Lane, Barnsley at 2am one cold January morning in a large ERF recovery lorry, also another recovery lorry set off to deliver a Leyland National for preservation, both setting off down the M1 motorway together. After a short stop to sort out the lorry heaters we soon left the other lorry behind, we arrived at the quarry where the bus was at 6.30am the driver then had his rest. Peter arrived about 8.00am, we loaded some spares, I paid peter for the bus, the driver changed the o/s rear tyre with one of the spare tyres that came with the bus as the original was unsuitable for the road. The bus was then lifted on suspended tow and manoeuvred out of the gate.
Collection did not go exactly to plan, on the M25 it found that the n/s rear wheel studs were giving way, so we tried to refit the front in to the rear wheel but they too tight and could not be undone, as the rear wheel had got warm we managed to remove some studs. So the bus was unhitched and away went the lorry to find some new studs, while I was left with the bus.
New studs were fitted, we hitched up the bus and away we went, unfortunately we had hitched the bus too close to the lorry and the o/s front corner of the bus caught the rear of the lorry on a corner in a service station. We arrived back at Geoff's yard in the evening, the bus stayed in Geoff's yard for a month while we got our premises ready, finally the bus arrived at our railway arch in February.
Our arch is rather cramped at 29ft wide and 66ft long and accommodates six buses these were at this time David Brundrit's ex Blackpool 540 a Leyland Titan PD3 with Metropolitan Cammel Weymann body, John Dyson's ex Sunderland 46 a Atkinson Alpha with Marshall body, Huddersfield Passenger Transport Groups Huddersfield 472 Daimler CVG6LX-30 with East Lancashire body and Huddersfield JOC 225 AEC Regent 111 with Northern Coachbuilders body, my ex Blackpool 300 with Burlingham centre entrance body, we also had Blackpool 510 which was being cannibalised for other buses.
A few days before the Sentinel arrived 510 was driven onto spare ground nearby (part of the deal with Geoff Ripley was that 510 went to him with its engine) other mechanical parts on the front axle were then removed along with parts of the breaking system, on the day the Sentinel arrived 472 and 225 had to be removed from the arch 225 decided that its fuel pump was not going to work (although it has been defective for a while it had run with out any problems a few days before) by manually moving the pump rack we moved it to a position where the recovery lorry could pull it out it too was put on the spare ground for a few hours.
The Sentinel was towed round and reversed into position on suspended tow we were pleased it went into the correct place at the first go. Then 225 was towed back round to the arch and placed as near as possible to its intended place. We thanked Geoffs driver and I left for work leaving the driver to hitch up the remains of 510, during this time 472 had been parked on a nearby street under the watchful eye of other arch tenants. Lenny and myself returned in the evening to adjust 225s position in the arch, by jacking it onto rollers to move the front sideways, when this was done 472 could be put away in the arch. Progress First the panel on the offside front corner was removed to assess the damage that was done on collection, it was found that the repair would not be too difficult, but it was also found that the interior panels were very rusty and they would require a extensive rebuild. As it was my intention to get the engine running early in the restoration it was decided that the offside front corner would be left for the present time. Also as the top step in the entrance was loose it was removed and stored for restoration. As the entrance door was not in place and was in the way inside the bus I decided to re-hang the door in place. The door was fitted, but only after replacement of the wooden body section which was mounted in the aluminium frame of the body.
The wooden body section was completely rotten and came out in several parts, the new piece of wood was made exactly to the shape of the aluminium frame, as the aluminium frame was in excellent condition I did not want to dismantle it to get the wood in place. With the panels in the doorway prised back the wood was forced into place, fortunately I had made the wood exactly the correct shape therefore it was a perfect fit. the panels were re-riveted in place some into the wood, a practice I have not come across before but as it worked originally when the bus was built, It was successfully done again.
The panels on the door were refitted where they had come loose and the door was hung on a new piano hinge as the original was missing but this was 6ins shorter. the door guides were overhauled as were the guide rollers and locating pins, as the bottom rollers were in bad condition they were swapped with the top ones, as the top ones carried no load, the bottom ones carry the weight of the doors. The bottom step was cleaned up to allow efficient operation of the door.
The emergency door was hanging on one hinge (the lower one), I have tried to purchase a new hinge, but I could not obtain one, so a repair the original was repaired this involved drilling out the broken pin, a smaller drill was used which eventually loosened the pin revealing the original pin hole. A new pin was made out of a long narrow bolt and fitted in place. The door handle is partly broken this has still to be repaired, but still will fasten the door in place.
Next it was intended to get the engine running, but it was found that the battery boxes were unfit to use so the intention of getting the engine running was not going to take place until new boxes were obtained. So preparations were made to fit new boxes, this involved rolling back the thick rubber floor covering, which revealed rotten floor boards and severely rusted battery box cradles so these were removed along with the spare wheel carrier which will be rebuilt later.
With the floor boards removed excellent access could be made to the chassis. The
main chassis is made of steel with aluminium outriggers to the body which were
bolted directly together. The rear overhang of the chassis was cleaned up and
repainted in hammerite, the cradles were rebuilt with new straps and angle iron
sides these were also hammerited and bolted back to the chassis, nothing was
done to the aluminium outriggers as they are in excellent condition and appear
to have never been painted.
The rear of the aluminium wheel boxes was cleaned up and a new steel rear support made which was bolted onto the chassis and body. I have made new floor boards painted them black similar to the original ones and fitted them in place. I have had made new battery boxes out of galvanised sheet and to save on cost I am fitting the original tops and drilling the cable holes myself.
Batteries were then fitted and on came the interior lights, which have since failed to operate, the wiring is in bad condition. A gear was then manually selected and with a long bar in the prop-shaft joint eventually I was able to turn over the engine for the first time since acquiring the bus, this eventually became easier. Then a starter motor was then fitted from former Blackpool 510 Leyland Titan PD3, the clutch was then released by jamming the clutch pedal down and by fitting a direct wire to the starter, the starter engaged and turned over the engine, after checking all was OK the engine was turned over for a long period of time until the batteries ran down, the engine turned over quite quick as there was no resistance with the fuel injectors removed. With this successful test the engine was now left as more work on the floor is required.
Moving forward along the bus the floor boards between the rear wheelboxes have been removed along with the floor trap over the differential. With this removed the rear axle, diff and springs have been cleaned up with a repair to the springs, then painted in hammerite paint including the aluminium casting of the diff as this appeared to have been painted when new.
Two large shock absorbers were cleaned up for repainting, but the nearside one sprang a leak while it being wire brushed, having survived the trip from Aldershot a few months earlier. The shock absorber was dismantled and welded up but as yet I have been unsuccessful in sealing it satisfactory, so the rebuild of the shock absorber was to go on, but I have found out that new ones are still available, so a new pair have been acquired, but are slightly narrower than the originals but are now in place.
The rear wheels have dirt plates on the inside, these have been removed, cleaned and repainted, but as a few rust holes appeared these were covered with a small piece of paper while the paint was still wet, then filled on the other side before that side is painted, this can save many hours making new parts when they are not load bearing.
Next the section of floor between the wheelboxes are ready for fitting new floor boards, the old floor trap will go back in place as it is still in good condition apart from a side edging strip that is missing, the front of the wheelboxes will require a new support bar to be made.
The next part of the restoration was to remove the old rotten floor boards above
the gearbox this was slightly more difficult than previous ones as they went
under a heating channel along the offside of the body. Once removed the
aluminium bodyframe outriggers could be inspected, once again these were
in excellent condition even though they were mounted direct to the steel chassis
frame. On the nearside some outriggers were slightly distorted as they also
carry the full weight of the fuel tank, the fuel tank was then removed for
repainting, and received four coats of silver hammerite paint this in
During this time the chassis and the gearbox were prepared and repainted. The
gearbox is a four speed manufactured by a company called "Moss" but is
incomplete as the side cover and the selectors are missing, I hope to acquire
the relevant parts in the near future but any help with these parts would be
appreciated.
Opportunity was also taken to overhaul the air cleaner which was in bad condition as it was the oil bath type, but was leaking oil, the steel bath part was removed and set on fire to remove oil and rust leaving several holes these were successfully rebuilt with plastic metal, it along with cleaner air dome was then repainted with Hammerite paint, the rest of the air cleaner is aluminium which was cleaned but not painted.
With the side cover missing and half shafts out I have been able to test all gears and they all appeared to operate well. Again new floor boards have been fitted, it was difficult to fit the ones under the heating channel but with brute force they went into place, but it was impossible to bolt them in place under the heating channel, but I have been able get some wood screw studs that look similar to the bolts used elsewhere.
Then came the shock news that the railway property company Spacia were to increase our rent by over 50%, first thoughts were close down, what are we spending this time and money for. Second thoughts were find somewhere else and continue, but I find it most rewarding seeing the progress as it is made. Spacia later accepted a 20% increase.
The vacuum tank was then removed and repainted over the six weeks, Back to work on the chassis around the engine.
This was cleaned including the copper / brass pipe work for the fuel and braking system which was then varnished to avoid discolouring, opportunity was taken to clean the oil filters as access was easier with the vacuum tank removed, the bottom of each filter mounting appears to be made of gunn metal these were cleaned and varnished. New seals were required these were home made from cardboard fruit juice cartons, I have had success with these on a previously overhauled Leyland engine.
The vacuum pump was cleaned but as it was in good condition it was not painted similarly the fuel pump was cleaned but was not in good condition but it was decided not to paint the fuel pump.
The engine rocker covers were removed and it was found that one of the rocker arms is missing along with the rods, so this has put back operation of the engine until these parts have been located, also the injectors were put back in the engine but one of these is incomplete. After drilling out broken studs and replacing with new studs, other engine parts missing are the injector pipes and the return fuel pipes.
The inlet manifold was removed and as it had a large hole in it, it was then subject to having a patch welded into it after painting the patch was well disguised. the outlet manifold was also removed as the bolts holding it in position were almost non existent. With the manifolds removed it was then decided to clean the inlet mounting chambers which appeared to be made on gunn metal these were cleaned and refitted as were the manifolds.
A exhaust pipe and silencer was then fitted which came from former Blackpool 510, also from 510 was the trackrod which was put in place, this fits better than the Sentinel track rod ends which came with the bus, the Sentinel ones are obviously the wrong ones and would have fouled the front springs. The vacuum tank was then refitted after repairs to the mounting straps and the outriggers for the tank, some of the vacuum pipes are still to be reconnected.
Once again the new floor boards were fitted, these were easier to fit than some of the previous ones as they would slide under the heating channel, but the finishing touches will have to wait until the final section is complete. The floor flaps were placed back in place.
A large heating channel was mounted on top of the box and part of the was also removed, the box once contained the heating radiator but this is now missing. The heating should work by collection of cold air from two large vents externally on the roof, this air is channelled down the back of the cab to a heating radiator under the drivers seat. The now warm air is channelled out of the back of the cab down a heating channel along the offside of the bus, this radiator is missing and it is not known what it looks like so one from a Leyland Atlantean has been acquired. The fuse box was removed and most wires marked for refitting, although most wiring will require replacing as it is in bad condition.
To remove the radiator the front lower panel had to be removed, this carried chrome trim which had to be removed first to give access to the trim the majority of the cab interior including the remaining thick aluminium floor. To give more access to the chassis the radiator was then removed, this is in bad condition it has had a extensive rebuild and is now back in place, although the vertical pipes still have to be re-fitted. This left the fan and fan drive loose, with great difficulty this was also removed.
The towing eyes are of a loop type bolted to the front and underside of the chassis, these are well rusted and would not be reliable in use. As the towing eye bolt holes on the front of the chassis are of similar spacing to Leyland Atlantean screw type towing eyes two of these have been acquired and have been fitted in place but have had to be ground shorter as they stuck-out forward of the body. The nearside chassis strengthener is in bad condition and has been removed and overhauled. The one on the offside is in good condition, so it will remain in place while the chassis is overhauled. It was decided to now renovate the whole of the cab at this time so the cab roof panel was removed so that the dented external roof dome could knocked back straight, as photographs show it was damaged early in its life. To knock back the roof a piece of soft wood was used being hit by the hammer as direct hammering was not possible. The interior lighting fuse box was renovated at this time along with some re-wiring to the bell, bell pushes and interior lights
Internal trim around both windscreens was now removed, the offside screen was completely removed as the sloping frame requires replacing, the external chrome strip fractured at every screw hole as it was removed, so a new strip will have to be made later.
All panels in the upper cab area along with the doors now had all the paint removed and filled as necessary with metal filler where corrosion had taken place, and repainted. New metal has had to be purchased to make a new sloping frame for mounting the offside windscreen, this will be difficult to make as there are different angles to take into account to make a new frame. It will take at over a year of my free time to renovate the front section of the bus as some of it is in bad condition.
The new windscreen frame has now been built and fitted it was necessary to fit the floor frame, this has now been re-built, as this has to be lifted over the steering column, and the windscreen frame would also be in the way, it was also necessary to remove the steering wheel.
The main fuse box is now under renovation which involves freeing off of switches including the mains switch which was solid, all internal wires are in good condition, the box now has been painted and refitted. The cab has been painted, but the seat box has still has to be made, the entrance panels have been recovered with Rexene, the top entrance step is now being replaced. Some of the Sentinel’s stable mates have changed, my Blackpool 300 bus, the one of Huddersfield buses are still there, they have been joined by another Huddersfield AEC Regent III with East Lancs body and a Bradford trolleybus.
In the H.C.V.S. May 2003 magazine a Sentinel generator unit was advertised for sale, very quickly a offer was made on the unseen generator unit after a description over the phone, it is powered by a Sentinel 4 cylinder engine which it is hoped will provide most of missing parts for ODE182’ engine (ODE182’s engine is 6 cylinder).
I hired a small truck and went to collect the generator unit from Lancashire, the unit was larger than expected at 10ft long, 4ft wide and 5ft high, it just fitted on the truck loaded by a tractor with rear mounted forks. I was wondering how I was going to unload such a large unit when I arrived back at our railway arch in Huddersfield, upon arrival the nearby woodyard’s fork lift truck was moving some wood in the street so I got assistance from the fork lift truck to unload and put the generator unit in our arch. I had only made a space of 8ft for the generator unit; this was quickly made larger to accommodate the unit.
The generator is quite old but appears to be in good condition as it has recently been rewired, I have had it running and runs well, once the Sentinel engine has been removed the remains are for sale, it seems that the unit would easily take a modern 4 cylinder engine to get it operational again, it is fitted with a Coventry Radiator.
It will be awhile before this happens as the cab of ODE182 has to be finished first.
|
|
|
|
|
|
|
|
|
|
|
|
|
#